Boost levels were same after mapping as running in, around 1.2Bar
as you can see from the pics its a right state, prior to mapping the cylinders were 170psi, no smoke etc out the back. Injectors have since been proved as fully functional as well. He did say that when it was being mapped the idle was all over the place 800-1600rpm.
He suspects major borewashing of number 3 cylinder, but what do you guys reckon happened, if you need more info il try and get some for you?
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